A failure of a first stage compressor blade of a Gas Turbine Generator in a Gas Treatment plant caused severe mechanical damage to the compressor section and power supply troubles. In this paper, the blade failure is investigated by mechanical, metallography and chemical analysis. A finite element analysis is performed on the blade geometry to identify the stress con- centration areas and the stress/strain values. The investigation outcomes provided the most probable cause of the premature blade failure and the recommendations to mitigate such inci- dents